Everything you never knew you wanted to know about the Mercury Project
LJ-5B
From RixWiki
Description of Mission
From SP-45 Mercury project summary
The Little Joe 5B vehicle was launched on April 28, 1961, from the Wallops Station launch site. The vehicle was composed of Mercury production spacecraft 14A and the seventh Little Joe launch vehicle to be flown. The spacecraft, which had previously been used for the Little Joe 5A mission, had been refurbished with only those systems installed that were required for the mission. There was no landing bag and certain other nonessential systems were missing. It was the first spacecraft to be flight-tested with modified spacecraft-adapter clamp-ring limit-switch mountings and fairings. Also, the sequential system was modified to prevent the limit switches on the spacecraft-launch-vehicle clamp ring or the spacecraft-escape-tower clamp ring from closing any circuits which would ignite the escape rocket until the band separation bolts were fired. These changes in and around the spacecraft-launch-vehicle interface and in the sequential system were made as the result of the problems encountered in missions Little Joe 5 and Little Joe 5A. Because of a severe change in flight path as the result of the delayed ignition of one of the two main launch-vehicle rocket motors, the test was made at substantially more severe flight conditions than planned. The abort was planned to be initiated at a dynamic pressure of 990 lb/sq ft; instead the dynamic pressure had attained a value of about 1,920 Ib/sq ft when the abort was initiated. However, the spacecraft escape system worked as planned and this test successfully demonstrated the structural integrity of the Mercury spacecraft. The spacecraft landed in the ocean after about 5 minutes of flight and was recovered and returned to the launch site in less than 30 minutes after launch. Analyses of the flight data and inspection of the spacecraft after the mission showed the spacecraft to be in good condition. An anomaly that showed up was the failure of two of the small spacecraft umbilicals to eject. Evidence indicated that these umbilicals failed to eject because of interference with the clamp-ring fairing after its release. This condition was corrected by changing the manner in which the fairing was supported on subsequent spacecraft. All test objectives were considered to have been met.

